- Joined
- Dec 3, 2016
- Messages
- 232
- City
- riverview, fl
- Vehicle Year
- 1988
- Engine
- 2.9 V6
- Transmission
- Automatic
- Total Lift
- none but it is a convertible
- Tire Size
- stock
or The ongoing story of how i've been screwed
in may of 2016 i had aamco put a 'factory rebuilt' trannie in my 95 2,3 auto ranger took a week and a half to get the truck back. there was an annoying thump from 2 to 3rd gear. aamco said its suppost to do that so you dont burn out the bands.(wdf?)
sept 2016 i went back for the umteenth time to bitch and there was a new manager who said'we're going to take care of you. they pulled the trans and got another. a week plus of no truck. when i got it back, it STILL had the thump from 2nd to 3rd. aamco said i had low vaacum in 3rd gear and they wouldnt do trans work until i did motor work first.
a few months ago, naybe april or may or 2017 i finally contacted aamco corporate who backed up the local shop but did say the local shop would swap a motor for free (i just had to supply the motor. the old motor was still running fairly strong)
august 2017. the 23rd the trans went into neutral 3 times in 2 minutes.
2 days later it did it again but then lost overdrive and would not upshift. and started leaking from the bellhousing.
dropped it at aamco on the 28th. not ready on september 1 so no truck for the holiday weekend wasn't ready until the 6th, wednesday
i picked the truck up at 4;30 on wednesday. on the shop window was a sign saying they would be closed until after hurricane irma passed. off i drove
2 times on the way home the trans 'flared'- momentarilly went into neutral, or maybe the converter unlocked, and then went right back into gear.
thursday morning on the way to work it flared again
thursday afternoon it made it less than 3 miles until, leaving a stop light, it would not shift into 2nd until 35 mph. next light that shift happened at almost 40. i thought the motor was finally going to grenade
the last light on the way home was red, as always. the truck stayed in first, wound up tight and barely doing 3 miles an hour
pulled into the yard, started the usual 3 point turn to face the gate-no reverse.
less than 24 hours and 75 miles and the trans is nfg
typed an explanation to aamco corporate of why i want a full refund and for them to take their piece of junk trans out of my truck. cant send it because the edress i used before when typing with them is no longer valid
no way to get out of the path of irma-i'm outside of tampa, and no way to get to a shelter so we are hunkered down riding it out
in may of 2016 i had aamco put a 'factory rebuilt' trannie in my 95 2,3 auto ranger took a week and a half to get the truck back. there was an annoying thump from 2 to 3rd gear. aamco said its suppost to do that so you dont burn out the bands.(wdf?)
sept 2016 i went back for the umteenth time to bitch and there was a new manager who said'we're going to take care of you. they pulled the trans and got another. a week plus of no truck. when i got it back, it STILL had the thump from 2nd to 3rd. aamco said i had low vaacum in 3rd gear and they wouldnt do trans work until i did motor work first.
a few months ago, naybe april or may or 2017 i finally contacted aamco corporate who backed up the local shop but did say the local shop would swap a motor for free (i just had to supply the motor. the old motor was still running fairly strong)
august 2017. the 23rd the trans went into neutral 3 times in 2 minutes.
2 days later it did it again but then lost overdrive and would not upshift. and started leaking from the bellhousing.
dropped it at aamco on the 28th. not ready on september 1 so no truck for the holiday weekend wasn't ready until the 6th, wednesday
i picked the truck up at 4;30 on wednesday. on the shop window was a sign saying they would be closed until after hurricane irma passed. off i drove
2 times on the way home the trans 'flared'- momentarilly went into neutral, or maybe the converter unlocked, and then went right back into gear.
thursday morning on the way to work it flared again
thursday afternoon it made it less than 3 miles until, leaving a stop light, it would not shift into 2nd until 35 mph. next light that shift happened at almost 40. i thought the motor was finally going to grenade
the last light on the way home was red, as always. the truck stayed in first, wound up tight and barely doing 3 miles an hour
pulled into the yard, started the usual 3 point turn to face the gate-no reverse.
less than 24 hours and 75 miles and the trans is nfg
typed an explanation to aamco corporate of why i want a full refund and for them to take their piece of junk trans out of my truck. cant send it because the edress i used before when typing with them is no longer valid
no way to get out of the path of irma-i'm outside of tampa, and no way to get to a shelter so we are hunkered down riding it out