Derf_the_Mule
New Member
- Joined
- Dec 9, 2014
- Messages
- 60
- Reaction score
- 0
- Points
- 0
- Location
- SouthWest Florida
- Vehicle Year
- 2007
- Make / Model
- Ford
- Engine Size
- 3.0L
- Transmission
- Automatic
The 2007 Ranger Sport I bought in October this year has been a money pit. I am ready to sell it and keep my '98 Ranger.
Haven't solved the random misfire and stumble on acceleration problem yet. I have fixed several others. I am surprised the PO was able to drive it. It was short 2.5 quarts of oil when my mechanic looked at it before I bought it. I should have run away then.
Problem 1: Misfire Cylinder #3 code popped up driving the truck home. It got much worse and started the flashing MIL after several weeks.
~Solution: Replaced Plugs with Motorcraft SP-413 gapped to 0.052" per owners manual (notice this conflicts with the Ford Workshop Manual)
~Solution: Replaces OE plug wires with Airtex wires.
Resolution: No more specific cylinder misfire or code. I can drive it now.
Problem 2: Random mild misfire, runs rough, poor acceleration, loud screaming noise near Cylinder #3.
Paid a Mechanic to check transmission codes with expensive Scanner. Asked him to find squealing noise near rear of engine.
Diagnosis: Vacuum leak in upper intake manifold gasket, sticking injector, misfire at startup (no cyl given)
Recommendation: Fuel rail flush first then replace injector(s) if still bad. Replace upper manifold gaskets (figure 8 shaped rubber)
~Solution: Replaced Fuel filter with Motorcraft. 3 fuel treatments added to gas.
~Solution: Found noisy Crankshaft Synchronizer, replaced with Motorcraft part. I did not replace the sensor. I reused the old undamaged sensor. The Sync was only noisy without any damage or excessive play.
~Solution: After not being able to find anyone to do a fuel rail flush correctly (I paid Valvoline quick lube place here $65 to do what they told me was a fuel rail flush, but was not. I found out after I paid.) I pulled the injectors, ohm tested them (12.4-12.6 ohms), then had them cleaned and flow tested at a local marina. Flow test before 77,77,77,76,76,76, replaced baskets, ultrasonically cleaned, replaced o-rings, flow test after 77 all.
~Solution: Replaced upper intake manifold gaskets, replaced valve cover gaskets since I had the plenum out of the way. They were leaking a little oil and I wanted to see the valves anyway. Cleaned out the electric heated PCV valve with brake cleaner (did not remove valve from cover). The oil on the valves was dark near the PCV valve (cyl 5+6). Replaced the PCV hose on the other side as well with Motorcraft part.
Resolution: No more squealing noise. Fuel pressure steady at 68psi, 5+psi shaking needle gone.
Problem 3: Random misfire that does not set a code, runs rough at idle, stumbles at WOT from fully closed (before rev limiter kicks in) cold, warm, and hot. KOEO Fuel pressure 10-30psi (not sure what this means, haven't found any significance to it yet), KOER fuel pressure 65-68psi, Ford Workshop manual says both between 65-75psi. Fuel pressure bleeds down to 0 after about 30-45 minutes after shutting off the ignition. Driving fuel pressure steady at 68 psi did not notice any variation. The needle started shaking a little over 2-4psi range can't tell if it happens when the engine shakes from the misfire.
~Solution: Tested TPS resistance with analog meter and voltage KOEO with digital meter. No abnormalities found 0.9-4.6VDC, ohm test moved needle steadily.
~Solution: Ran fuel pump on override switch key off for 5+ min, disconnected ignition from coil, turned over engine to get any leaking fuel into cylinders, checked for wet plugs. No plugs were wet or smelled of gas. The fuel pump pulls 6.4 amps KOEO and 7.4 amps KOER. I suspect the fuel pressure regulator and/or pump check valve are leaking, but I cannot confirm it.
~Solution: Check compression: Completed test then read more carefully that test should be done at operating temp. I drove truck for 20 minutes. Then put a fan over the exhaust manifolds to lessen the burns and blisters. Compression test results: 10 cycles cold, 6 cycles hot, cyl-dry cold/wet cold/dry hot/wet hot 1-190/250/200/230, 2-192/260/207/240, 3-185/255/197/232, 4-162/210/190/211, 5-198/280/200/228, 6-190/285/207/235. Hot-dry test showed 8.2% H-L well within spec. Hot-wet test showed 13.7% H-L again well within spec. Cold tests showed 19-36% H-L assuming invalid. I don't have enough experience to interpret beyond.
~Solution: Check for vacuum leaks with water, can't find any, check EGR for leaks/ malfunctions. EGR appears to be working normally. Replaced DPFE sensor (I discovered it wasn't causing the problem when I left the vacuum line off the EGR solenoid, but I broke the old one removing it). I cannot verify the EGR solenoid function because my vacuum gauge does not read in the operating range of the solenoid (0-10 inHg). No vacuum leaks found.
~Solution: Check IAC valve. Tested OK according to manual. Cleaned it out with carb cleaner. No change. The engine nearly stalls when IAC is disconnected. Normal function as far as I can tell.
~Solution: Checked for bad plug wire from new set by replacing wire one at a time with old OE wire. No change. Re-gap plugs to 0.043" per Ford Workshop Manual (conflicts with owners manual, emissions sticker says see specifications for gap). Stumble on WOT improved. Possible backfire still present, but harder to get.
~Solution: Tested coil pack with 2 OTC HEI testers. Showed plenty of spark all 6 cylinders.
Resolution: Need help. Light backfire still present or worse back pressure from plugged cats. Could really use some help on this. I don't want to destroy my cats. It is possible the cats are already clogged from the fuel treatment done by the Valvoline quick lube place or from spraying a small amount of carb cleaner onto the valves when the injectors were out. I would not be opposed to cleaning the cats with the lacquer thinner method, but I am a little unsure about it damaging something in the fuel system.
Next step(s): Remove O2 sensor(s) to observe back pressure, any other suggestions??? Tried removing O2 sensors. I don't have a wrench big enough to get leverage.
I am sure there are things I've done not listed. I've been beating my head over this for 3+ weeks. I am out of money replacing parts and buying testing tools. My code reader does not take live data, it only reads engine codes and clears codes.
Haven't solved the random misfire and stumble on acceleration problem yet. I have fixed several others. I am surprised the PO was able to drive it. It was short 2.5 quarts of oil when my mechanic looked at it before I bought it. I should have run away then.
Problem 1: Misfire Cylinder #3 code popped up driving the truck home. It got much worse and started the flashing MIL after several weeks.
~Solution: Replaced Plugs with Motorcraft SP-413 gapped to 0.052" per owners manual (notice this conflicts with the Ford Workshop Manual)
~Solution: Replaces OE plug wires with Airtex wires.
Resolution: No more specific cylinder misfire or code. I can drive it now.
Problem 2: Random mild misfire, runs rough, poor acceleration, loud screaming noise near Cylinder #3.
Paid a Mechanic to check transmission codes with expensive Scanner. Asked him to find squealing noise near rear of engine.
Diagnosis: Vacuum leak in upper intake manifold gasket, sticking injector, misfire at startup (no cyl given)
Recommendation: Fuel rail flush first then replace injector(s) if still bad. Replace upper manifold gaskets (figure 8 shaped rubber)
~Solution: Replaced Fuel filter with Motorcraft. 3 fuel treatments added to gas.
~Solution: Found noisy Crankshaft Synchronizer, replaced with Motorcraft part. I did not replace the sensor. I reused the old undamaged sensor. The Sync was only noisy without any damage or excessive play.
~Solution: After not being able to find anyone to do a fuel rail flush correctly (I paid Valvoline quick lube place here $65 to do what they told me was a fuel rail flush, but was not. I found out after I paid.) I pulled the injectors, ohm tested them (12.4-12.6 ohms), then had them cleaned and flow tested at a local marina. Flow test before 77,77,77,76,76,76, replaced baskets, ultrasonically cleaned, replaced o-rings, flow test after 77 all.
~Solution: Replaced upper intake manifold gaskets, replaced valve cover gaskets since I had the plenum out of the way. They were leaking a little oil and I wanted to see the valves anyway. Cleaned out the electric heated PCV valve with brake cleaner (did not remove valve from cover). The oil on the valves was dark near the PCV valve (cyl 5+6). Replaced the PCV hose on the other side as well with Motorcraft part.
Resolution: No more squealing noise. Fuel pressure steady at 68psi, 5+psi shaking needle gone.
Problem 3: Random misfire that does not set a code, runs rough at idle, stumbles at WOT from fully closed (before rev limiter kicks in) cold, warm, and hot. KOEO Fuel pressure 10-30psi (not sure what this means, haven't found any significance to it yet), KOER fuel pressure 65-68psi, Ford Workshop manual says both between 65-75psi. Fuel pressure bleeds down to 0 after about 30-45 minutes after shutting off the ignition. Driving fuel pressure steady at 68 psi did not notice any variation. The needle started shaking a little over 2-4psi range can't tell if it happens when the engine shakes from the misfire.
~Solution: Tested TPS resistance with analog meter and voltage KOEO with digital meter. No abnormalities found 0.9-4.6VDC, ohm test moved needle steadily.
~Solution: Ran fuel pump on override switch key off for 5+ min, disconnected ignition from coil, turned over engine to get any leaking fuel into cylinders, checked for wet plugs. No plugs were wet or smelled of gas. The fuel pump pulls 6.4 amps KOEO and 7.4 amps KOER. I suspect the fuel pressure regulator and/or pump check valve are leaking, but I cannot confirm it.
~Solution: Check compression: Completed test then read more carefully that test should be done at operating temp. I drove truck for 20 minutes. Then put a fan over the exhaust manifolds to lessen the burns and blisters. Compression test results: 10 cycles cold, 6 cycles hot, cyl-dry cold/wet cold/dry hot/wet hot 1-190/250/200/230, 2-192/260/207/240, 3-185/255/197/232, 4-162/210/190/211, 5-198/280/200/228, 6-190/285/207/235. Hot-dry test showed 8.2% H-L well within spec. Hot-wet test showed 13.7% H-L again well within spec. Cold tests showed 19-36% H-L assuming invalid. I don't have enough experience to interpret beyond.
~Solution: Check for vacuum leaks with water, can't find any, check EGR for leaks/ malfunctions. EGR appears to be working normally. Replaced DPFE sensor (I discovered it wasn't causing the problem when I left the vacuum line off the EGR solenoid, but I broke the old one removing it). I cannot verify the EGR solenoid function because my vacuum gauge does not read in the operating range of the solenoid (0-10 inHg). No vacuum leaks found.
~Solution: Check IAC valve. Tested OK according to manual. Cleaned it out with carb cleaner. No change. The engine nearly stalls when IAC is disconnected. Normal function as far as I can tell.
~Solution: Checked for bad plug wire from new set by replacing wire one at a time with old OE wire. No change. Re-gap plugs to 0.043" per Ford Workshop Manual (conflicts with owners manual, emissions sticker says see specifications for gap). Stumble on WOT improved. Possible backfire still present, but harder to get.
~Solution: Tested coil pack with 2 OTC HEI testers. Showed plenty of spark all 6 cylinders.
Resolution: Need help. Light backfire still present or worse back pressure from plugged cats. Could really use some help on this. I don't want to destroy my cats. It is possible the cats are already clogged from the fuel treatment done by the Valvoline quick lube place or from spraying a small amount of carb cleaner onto the valves when the injectors were out. I would not be opposed to cleaning the cats with the lacquer thinner method, but I am a little unsure about it damaging something in the fuel system.
Next step(s): Remove O2 sensor(s) to observe back pressure, any other suggestions??? Tried removing O2 sensors. I don't have a wrench big enough to get leverage.
I am sure there are things I've done not listed. I've been beating my head over this for 3+ weeks. I am out of money replacing parts and buying testing tools. My code reader does not take live data, it only reads engine codes and clears codes.
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