Failing all other attempts to make an engine in an '88 Bronco2 run right
and this included PROPER diagnostic proceedure followed by systematic
replacement of ALL the modules with others from a running (perfectly running)
2.9 that were thus "known good" and having all attempts fail the last step was to REMOVE the entire engine management harness from the patient and get another complete harness from a junkyard vehicle.
After doing that and determining something inside the removed harness was broken
because it FIXED the problem, no further examination of the removed harness
was conducted.
The problem was solved, the harness was fukt, nobody had enough
energy to ponder it any further.
It soon became a toot point as the bronco2 in question was subsequently
rear ended while making a Right hand turn by a drunk in a firebird and flipped
end-over several times.... making further research doubly pointless.
AD