Ok- made it back to my dad’s in the heated garage for round 2. I am leaving for a trip tomorrow, so I couldn’t bear wondering if I did it right- how would it change.
New test wot and hot engine.
1-10
2- 20
3-100
4- 25
5- 75
6- 50
It is not a wore out engine- that is what is odd. At 38k miles ago, I put in a new remanned motorcraft short block that I had bought off a guy who never used it in a crate. Insides looked spanking new. It had set in a crate for probably 5 years when I got it, it probably set in my possession for 10. It was crated in plastic wrapping soaked in oil. I installed everything new I could possibly think of when I put it back together.
the old engine wasn’t having any problems except it was leaking like a ford. It was wore out from the miles- but it never gave me any issues. It went 314k.
ha. The heads were a bit of a challenge. Because it was a 2000 style block, I had to use 95tm heads to keep it stock compression. I found some loaded nos units on eBay, but when I got them they were 93tm. So i found some 95tms and had a local machine shop go through them and swap the valve hardware.
when i assembled it, it had a noise in the valves. So I took the heads off and took them back to the machine shop. They said they went through everything and it was fine, but that they hand lapped them just to be sure.
I swapped to nos ford lifters from new ones melling ones I bought and installed and the noise went away.
So it still idled odd, but ran ok and I have been driving and tinkering with it.
Any thoughts on what low compression in all cylinders would be? I am wondering if the valves and heads have issues. Might pull them and take them to another machine shop. Sucks.