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I had an 88 blazer with a 350, had the same issue. The clutch fork pivot ball was worn almost flat, essentially moving the fork 'back' about 1/8 of an inch. This took travel away from the slave end of the fork and from the throw out end.
The fork shouldn't be coming anywhere near the belhousing...which makes me think the fork is too far 'back', so the slave cant push it far enough to pivot the other end far enough...
It should be threaded into the tranny..you could try backing it out a few threads, to give the fork more travel on both ends.
The other thing it could be is air in the system...but it sounds like you've got it pretty well bled.
You can pull the fork without pulling the tranny, cant you?
You know what it is?
It,s the chevy gods. They are mad because you put a ford body on one of their frames. Wish I could be more help.
i just got the call, the ball was not excessively worn but it was fairly worn, nor was the flywheel excessively machined but it was getting close. and the aftermarket clutch fork was slightly different in the way it was manufactured from the one i pulled out. (.010" he said)
no one of those things would have been enough to cause my problem. but added together was what it took. a slightly taller pivot ball was all it took to solve it all 350 f-ing dollars later
yeah transmaster did it, i had him do it because he said "for a 1hr diag i will tell you what's wrong or i won't charge you" and he stuck to his word despite spending what i would wager to be a lot longer than an hour on it. he couldn't because he needed to pull the trans and mike out everything so he then said "no charge, but for $350 i promise i'll fix it, or no charge....." after all my dicking with it $350 seemed worth it. and its fixed now but i can't go get it until tomorrow when i get paid
i just got the call, the ball was not excessively worn but it was fairly worn, nor was the flywheel excessively machined but it was getting close. and the aftermarket clutch fork was slightly different in the way it was manufactured from the one i pulled out. (.010" he said)
no one of those things would have been enough to cause my problem. but added together was what it took. a slightly taller pivot ball was all it took to solve it all 350 f-ing dollars later