update.
Last week, I got the injectors back, and 2 of them had poor flow, 2 had fair flow. One of the poor flowing injectors had a drip leak. Before the rebuild, they were mismatched within 22.2% of amount of flow between the 4 of them, and after the rebuild, the flow is good and they are matched within 1.1%.
Put those in, and still had a code for idle air control error, so we replaced the idle air control valve, reset the computer and it seemed to run okay, but still had a misfire.
I had driven it about 100 miles yesterday, and the check engine light had not come on so I got the code reader and it showed no codes, and that it would pass smog. I immediately took it to the smog place, and it passed with flying colors. It's hilarious that the check engine light came right back on 2 minutes after I left the smog place!!!!!!

it was a code for the idle air control error again...most likely for high idle as it was idling at 1200rpm, so I backed the idle screw off to 800rpm and reset the computer, and it hasn't come on again....yet.
I have an appointment with the dmv to get my tags today, and we'll be back in business, and no more back-up cars or back-up cars for my back-up car.
It still had a misfire though, and we figured that it is probably one of the coils. My dad's thunderbird's coils are the same part number so we swapped them out last night, and the truck ran really smooth, no misfire.
Hate to jinx it, but I think that it's fixed.