rangerin
Well-Known Member
I just finished swapping the auto trans out for a M50D in my '84 ranger. While at it, I took the motor out and tore it all apart to clean it and do a full reseal. I did take the carb apart, but only a little. I changed a few gaskets that were leaking, but I didn't remove any mixture screws or anything that would "mess it up".
Problem: I can't bring the idle down at all. I checked for vacuum leaks and have none. In the past, the truck would hold a steady 20 inHg at idle. Right now, its barley gets 11 inHg at idle. Also, the motor knocks a little just before dying when I bring the idle down via the idle speed screw. I've tried messing with the two air/fuel mixture screws, but can't get any improvement there either. The distributor is set correctly also. Any help is much appreciated as I've been working on the truck everyday for 2.5 weeks and I just want to drive it!
Truck specs:
2.8 motor
Holley carb
Durasparked (as a result, all emmision stuff ripped out)
Timed to 12 degrees (truck runs better @ 12 since durasparking)
Problem: I can't bring the idle down at all. I checked for vacuum leaks and have none. In the past, the truck would hold a steady 20 inHg at idle. Right now, its barley gets 11 inHg at idle. Also, the motor knocks a little just before dying when I bring the idle down via the idle speed screw. I've tried messing with the two air/fuel mixture screws, but can't get any improvement there either. The distributor is set correctly also. Any help is much appreciated as I've been working on the truck everyday for 2.5 weeks and I just want to drive it!

Truck specs:
2.8 motor
Holley carb
Durasparked (as a result, all emmision stuff ripped out)
Timed to 12 degrees (truck runs better @ 12 since durasparking)
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