- Joined
- Jan 28, 2022
- Messages
- 7
- Reaction score
- 1
- Points
- 3
- Age
- 63
- Location
- Lacey WA
- Vehicle Year
- 1994
- Make / Model
- Ford Ranger XLT
- Engine Type
- 4.0 V6
- Transmission
- Manual
- 2WD / 4WD
- 4WD
- Total Lift
- 2 inch leveling kit
- Tire Size
- 31×10.50
My 94 Ranger was running just fine then one day developed a very rough idle and misfires. Ive replaced plugs wires and coil pack no help. Cleaned the MAF sensor and IAC. All were no help. No vaccum leaks, No fuel in FPR vaccum line and no vaccum leaks detected using carb and choke cleaner at as many possible vaccum leak areas I could think of. Oh and no CEL. All six plugs indicated a rïch running condition.
Update...I removed PCM after testing with a scan tool. 513 DTC indicating internal voltage failure in the PCM. Upon removing the cover I found all three electrolytic capitors were leaking or damaged. Also found a blown resistor on the positive leg of the 10uf 63v capacitor. Bought a repair kit on Amazon and found a local electronics repair shop to do the repair. Only took him an hour and cost me $50. Installed back in the truck and still got the 513 DTC. But the truck seemed to run much better but still with a rough idle. I turned the truck off waited a couple minutes turned truck on without starting and used a stethoscope to verify pump was running in the tank and it was. Went to the fuel rail immediately after turning off the key and pushed the pin in on the fuel rail schrader valve. Fuel came out but was definitely not at 30+ psi. Only spurted out about two inches for less than a second. Am I looking at a bad pump or clogged fuel filter? The low pressure would explain the rough idle.
Update...I removed PCM after testing with a scan tool. 513 DTC indicating internal voltage failure in the PCM. Upon removing the cover I found all three electrolytic capitors were leaking or damaged. Also found a blown resistor on the positive leg of the 10uf 63v capacitor. Bought a repair kit on Amazon and found a local electronics repair shop to do the repair. Only took him an hour and cost me $50. Installed back in the truck and still got the 513 DTC. But the truck seemed to run much better but still with a rough idle. I turned the truck off waited a couple minutes turned truck on without starting and used a stethoscope to verify pump was running in the tank and it was. Went to the fuel rail immediately after turning off the key and pushed the pin in on the fuel rail schrader valve. Fuel came out but was definitely not at 30+ psi. Only spurted out about two inches for less than a second. Am I looking at a bad pump or clogged fuel filter? The low pressure would explain the rough idle.
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